CASE STUDY (1)

Well Info

  • JOB DESIGN – 9 5/8 – WBCO
  • Deviation – 55 ⁰
  • Well MD – 10 560 ’
  • Drilling Fluid – 10.8 – PPG OIL BASE MUD
  • Completion Fluid – 8.7 PPG NaCl2

Objective
Clean out cement positive negative Test – casing pickling and displace to completion fluid to save 24 hours from rig time.

Conventional Procedures

  • Run with WBCO for Casing Pickling and displacement)
  • Unconventional Procedures (Combining 2 Run in one trip and well ready for completion)

Services Provided
Mechanical Wellbore Cleanout Tools – Scraper – Brush – Magnet – Junk Basket

  • Technical Proposal
  • Displacement Chemicals
  • Tool Placement Design
  • Wellsite Engineering Supervision

Results
The following parameters; Fluid Interface, Volumes Circulated to desired fluid clarity, Total Circulating Time  and Diff. Pressure were all within  the value in the well program.

CASE STUDY (2)

Well Info

  • JOB DESIGN – 9 5/8 – WBCO
  • Deviation – 40 ⁰
  • Well MD – 12 560 ’
  • Drilling Fluid – 10.2 – PPG OIL BASE MUD
  • Completion Fluid – 9.2 PPG NaCl2

Objective

  • Conventional Procedures
  • 1- Run in with Bit clean out cement
  • Unconventional Procedures
  • Combining 3 Run in one trip and well ready for completion

Service Provided
Mechanical Wellbore Cleanout Tools – Scraper – Brush – Magnet – Junk Basket with Liner Top Testing Tools.

  • Technical Proposal
  • Displacement Chemicals
  • Tool Placement Design
  • Wellsite Engineering Supervision

Results
The following parameters: Fluid Interface, Volumes Circulated to desired fluid clarity, Total Circulating Time and Diff. Pressure were all within the value in the well program.

MSI Tools Value Additional
It estimated that MSI tools normally saves client over $220,000 per well.

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